Radio
Boulevard
Model ATD Contractor: Bendix Radio Division of Bendix Aviation Corporation SN: 2104 built by: Sparks-Withington Co. (Sparton)
ATD Basics, Mechanical Construction,
Electronic Requirements by: Henry Rogers WA7YBS |
ATD Components Shown in Artwork A - ATD Transmitter A - 200kc -500kc Tuning Module B - LF Antenna Tuner C - Dynamotor D - Pilot's Channel Indicator E - Pilot's Remote Control F - Dynamotor Battery Cable G - Transmitter Power Cable H - Remote Cable I - Indicator Cable |
B&W Artwork from the ATD Manual |
This write-up is a little bit different. All of the repairing, rebuilding and restoration is presented in a "day-by-day, problem-by-problem" journal format that also has included the solutions to the multitude of minor issues encountered. Of course, the ability to easily apply the voltages required at the current levels necessary for proper operation is one of the most difficult aspects of setting up a vintage aircraft transmitter to function effectively in a home environment or ham shack. Though a homebrew ART-13 AC power supply can operate the ATD, I've found that it's also not too difficult to set-up and use the ATD dynamotor to provide the proper voltages at the necessary current levels. However, the dynamotor's 50A+ "instantaneous starting current" can present problems. Fortunately, I found an easy solution and plans are included for an "easy-to-build" 80 AMP +28vdc power supply that can provide all the current necessary for dynamotor operation. Antenna matching solutions are easy to accomplish. There's also the fairly low RF output power that makes reception of the ATD's signal a challenge for many of the mil-rad net participants. How to boost the power output with a linear amplifier is also covered. |
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ATD History
- The story goes that, around 1940, the Navy was interested in
purchasing a newly
designed, modern aircraft
transmitter, mainly for their two-seater aircraft. Supposedly a
competition ensued between some of the manufacturers vying for a Navy
contract. Eventually, three different types of aircraft transmitters were
accepted and produced for the USN (some competition,...since all
three transmitters were given contracts.) RCA provided the very small ATB
transmitter. With only two selectable channels and only about 3.5 watts
output, RCA had decided that their transmitter would be used in
a two-seater for plane-to-plane communications. Bendix provided the ATD, a slightly
more powerful transmitter with motor-drive selecting of four frequency channels
that were pre-flight tuned. However, the ATD was still basically for the
two-seater aircraft but the 40-50 watts output could provide air-to-ground communication.
Collins provided the ATC, a versatile and powerful transmitter that could be used in
almost any installation. At 100 watts output with ten HF and one LF selectable
frequency channels that motor-drive auto-tuned the transmitter to preset
antenna matching, it really wasn't much of a surprise that the Navy
favored the ATC transmitter. It became
the famous ART-13 and it's likely that over 100,000 were built during the war
and thousands were used post-WWII by various airlines.
But, what about the Bendix ATD and the RCA ATB? There was only one ATD contract
dated May 20, 1940 but it seems that several orders were built on that
one contract during
WWII. The ATB is very rare so it must have had only one contract also. ATD Transmitters Post-WWII and Today - The total number of ATD transmitters built was probably much less than 5000 (serial numbers might go up to 4000 or so.) Many were never used and were still essentially new in their crates (packed with all their accessories) after WWII ended. Many of these "new in the crate" ATDs were sold surplus after the war. However, the ATD transmitter certainly wasn't a modern design and it wasn't suitable for use by post-WWII airlines like the ART-13 was. Its multitude of tiny-sized knobs and hidden adjustments made "in-flight" retuning impossible. >>> |
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>>> The ATD wasn't practical for ham radio
either. Working on an ATD was difficult due to
its multitude of relays and
other "moving" contacts that were always causing problems. Then there were
the four individual tuning units and the dense packaging of the main
frame that made maintaining an ATD as an operational transmitter a real
challenge.
Today, there seem to be three types of ATD survivors,...the "found in the crate" mint condition transmitters that were kept in NOS condition and were never worked on. These types of transmitters, despite their pristine physical condition, rarely function "out of the box." At the other end of the condition-spectrum are the hacked-up junkers that were the unfortunate victims of the readers (and believers) of the Surplus Conversion Manuals put out by CQ magazine. But, many ATD transmitters, while maybe not mint, are still in pretty good shape. These "less-than-perfect" transmitters haven't been hamster-hacked and they weren't converted into something else that wouldn't function either. The following sections of this write-up are a detailed account of what to expect from, maybe not perfect, but a pretty nice ATD. One that obviously wouldn't work "as-found" but looked like it might be coaxed into becoming a functional transmitter. Obvious problems are that only one of the tuning units matches the main frame serial number (so three tuning units are replacements for some reason,) the RF Amp meter is gone and all of the tubes except the 12SL7GT are gone. All of these clues are indications of a non-working unit that supplied a RF amp meter and some tubes for some other projects but was kept in relatively good condition,...well, except for the usual moving and storage cosmetic problems. So, let's see what it takes to get this relic of early WWII actually producing some RF,... |
ATD Basic Design and Construction |
Four channels were available for operation. The multitude of adjustments that were necessary for each channel to operate properly made "pre-flight radio setup" a prerequisite. Since any significant frequency adjustment of any channel required removing the channel's individual Tuning Unit from the main frame for resetting four internal switches followed by retuning the transmitter, any readjustment of settings during the flight wasn't practical and essentially couldn't be accomplished. The manual implies that neither the pilot nor the second person were necessarily "radiomen" but they could "operate" the transmitter within the limitations of the pre-flight setup. The fact that the REMOTE-LOCAL switch was "safety-wired" to REMOTE implies the second person in the airplane wasn't a trained radioman (the manual does refer to this person as "the operator" even though he can't directly operate the transmitter.) The frequency selection of the four channels was motor-driven based on the position of the channel switch on either the transmitter or its remote. A chain-driven rotating "letter wheel" (on the ATD) would display which channel had been selected. The selection of a channel's tuning module was accomplished by the motor driving a gearbox that slowly rotated a shaft that had four cams. The four cams with "roller tips" on the shaft were spaced at 90º increments and would individually would push down a specific rectangular push-rod for each channel as the shaft slowly rotated. The push-rod had several metal pins (~.25" diameter) that would push down the movable selector contacts on the back of the selected Tuning Unit to connect the various frequency controlling circuits and the antenna matching circuits for the channel selected. Unselected channel contacts were grounded by way of the spring-loading of the contact arms contacting metal grounding pins. The motor-drive used a forward and a reverse winding that was timed to use just a momentary "reverse" connection to stop the motor after the forward winding was disconnected. This allowed precise position stopping at the selected channel with no "over-shoot." There was a manual channel select knob on the right side of the transmitter. If the handle of this knob was folded out, that disengaged the motor drive gearbox and the main shaft could then be rotated using this knob. When finished with the manual adjustment, the knob was folded back, "rocked" slightly and then the manual control being "spring-loaded" would "drop into position" to engage the motor drive gearbox and to be in the correct position displaying the correct channel. >>> |
>>> The ATD uses a 6L6G tube as the Master Oscillator.
The Audio Driver and MCW/Sidetone oscillator functions are both accomplished by
another 6L6G. The Power Amplifier tube is an 814/VT154 with +1000vdc on
the plate. The two modulator tubes are a pair of 6L6G tubes provided
push-pull plate modulation of the 814 PA. A VT-150/0D3 tube is used for
a +150vdc voltage regulator for the MO screen voltage. A 12SL7GT is
hidden away behind a shield in the right side of the transmitter. The
12SL7GT is the speech amplifier and it uses one triode if a dynamic
microphone is used (250Z) or it uses both triodes if a carbon mike is
used. There are a multitude of relays in the ATD. The sending relay switches the antenna from receiver to transmitter with actuation of the sending key or PTT. The Phone relay selects many of the functions necessary for voice or MCW operation. CW selection places the +1000vdc on the 814 plate and +380vdc on the plates and screens of the other tubes but allows the telegraph key to work the keying line (PTT.) There's another relay that places a capacitor on the PA grid to keep it from oscillating when the TUNE mode is selected (it's switched out with PTT or keying.) There's a connecting strap between the TUNE and OPERATE switches so they will function together. The TUNE switch is isolated since it connects the +1000vdc when OPERATE is selected. The Grid Current Meter measures the MO plate output by its connection to the PA grid. This meter has a switch that allows it to also read battery voltage (the aircraft battery buss voltage.) The PA plate meter reads the plate current (cathode current) on the 814 tube. The RF Amps (Antenna Current) measures the actual RF current to the antenna (fs=5A.) Power output is normally 50 watts in CW and 40 watts in Phone.
The dynamotor provides +380vdc at 400mA and +1000vdc at 150mA. Input voltage is +28vdc and the current required depends upon the load but could range up to 19 amps in some modes and to certain types of antennas (this is the "up and running" current but the actual "instantaneous starting current" is around 50 amps.) The top cover that allow access to the tubes has an interlock switch that only allows the +28vdc to go to the dynamotor when the ATD lid is closed. The dynamotor also has an interlock on its top cover. The Cannon box connectors on the left side of the transmitter are for the dynamotor, the remote and for the channel indicator (a box with buttons that would protrude out if that channel was selected and would retract if another channel was selected and then that channel's button would protrude out. Both the remote and the indicator were up with the pilot.) The remote was operated by the pilot and had inputs for a mike and a key along with the ability to select channels. No meters or other indicators were on the remote. |
Mechanical Construction - The ATD is build around an aluminum framework that is spot-welded together to create a three section open box with a right side, a center section and a left side. The center section has a tube shelf at the rear, a bottom and an upper support for the motor drive shaft and the channel switching push rod assembly. Aluminum panels are screw-mounted to the two sides, the top and the bottom and these panels are painted black wrinkle finish (except for the bottom cover.) The front panel on the left is smooth flat black finish and contains the RF Amp meter and input jacks along with the Tune/Operate switch. The right panel is also smooth flat black finish and has the PA current meter and the PA Grid current meter that also measures Battery voltage along with the channel selector and channel indicator wheel. Mode selector switches and the OFF switch are also on the right side. Also on the right side but inside the main frame are the Sidetone volume control and the Microphone type selector switch. The rear part of the top cover is hinged and lifts up to allow access to the tubes. However, the 12SL7GT tube is located behind the right side panel and its only easy access requires removing a shield that is located on the inside of the center section (right side) with the Channel D module removed. The channel tuning modules contain all of the coils and capacitors necessary for the MO and the PA tuning. A lot of fiberboard (Garolite) construction is used and even the switch shafts are actually made out of fiberboard. The mounting rails have integral rubber shock mounts. Total weight of the ATD is 70 pounds. The external dimensions are 23"W x 11"H x 13.75"D. | Electronic Requirements - The ATD uses (1) 814, (4)
6L6G, (1) 0D3 and (1) 12SL7GT tubes. The 814 plate requires +1000vdc.
This is the only place that the +1000vdc is used. The two modulator
tubes, 6L6G, actually have +380vdc on their plates. The maximum rating
for the plate to cathode voltage on a 6L6G is around +380vdc so that was
the limitation of using 6L6G tubes as the modulators. The +380vdc is
also used on all four of the 6L6G screens and plates (with various
divider or load resistors) and also on the 814 screen. The 0D3/VT-150
provides +150vdc for just the MO screen voltage. +28vdc
operates the tube filaments and the relays. The dynamotor runs on the +28vdc aircraft battery buss. The +28vdc battery buss is also routed directly to the transmitter through the dynamotor and ATD power cable. When the ATD is powered up, it routes the +28vdc back to the dynamotor relay via the PTT line to power up the dynamotor to supply the +380vdc and the +1000vdc. CW operation will have the dynamotor running while the transmitter is keyed. In Phone, the PTT turns on the dynamotor for operation. AC Power Supply Operation - To run the ATD will require +1000vdc at about 150mA, +380vdc at about 400mA and +28vdc at maximum of about 20 amps for the dynamotor (this doesn't include the instantaneous starting current,) but only about 5 amps are required if the +28vdc just powers the transmitter. It's convenient that these voltages are very close to those required by the ART-13 transmitter. This makes operating the ATD using an ART-13 AC power supply a real possibility. The current requirement of 400mA on the +380vdc line might be a problem in some ART-13 power supplies (it depends on the design.) My "Homage a le Valve" ART-13 AC PS provides +1050vdc at 250mA, +420vdc at 250mA and +28vdc at 10A. I'll have to do some slight modifications to the +400vdc supply but whether the ATD actually requires almost half an amp on the +380vdc line will have to be determined when I actually get the transmitter operational. If the +380vdc actually does require 400mA then a separate +380vdc with higher current availability would be required. I do have the HP 713B that could supply +380vdc at 500mA, so that's a possibility,...if it becomes necessary. |
ATD Aircraft Transmitter SN: 2104 - Problems and Solutions This is more-or-less a chronological listing of what it took to get the ATD to actually produce a RF signal into an antenna. Dates are at the end of each paragraph. |
Missing Antenna Current Meter - This is a 5 amp FS
meter that has an internal shunt that allows connecting the RF directly to and
through the meter out to the antenna post. The meter is recessed behind a
standard bakelite meter flange, glass and partial housing. About 1" of the
housing allows the actual Antenna Current meter to mount behind the empty meter
housing and that gives the actual meter the spacing necessary. It's possible
that the actual meter
mounted with four standoffs but what the meter itself mounted to is not known
and there aren't any photos available of an original installation. I assume that
fiber board was used. The actual meter's flange has to be cut on the right side
to provide proper clearance to "center" the meter mounting and have the meter
scale centered in the front meter housing (it doesn't seem likely that the
installation would require modifying the meter flange - but it does!) Also, the meter I have is out of an
ART-13, so the scale is marked "ANTENNA CURRENT" while the original meters were
marked "RF AMPERES." 8-17-24 UPDATE: W7MS,
who also owns an operational ATD transmitter, is going
to donate a 5A RF current meter out of a "parts set" Bendix TA-12.
This meter has the proper spacer for recessed mounting but uses only the three
meter flange screws. The scale will have to be changed since it's a white scale.
The ART-13 meter scale should fit. According to Mike-MS, the four outer
perimeter holes were for mounting a metal cup-like shield that covers the meter
(actually only three screws were used since the top-left screw threads into the
main frame. I'll pick up the Bendix meter at
the SNARS Fall Cabela's Swap Meet a few weeks away.
The Plate Current Meter had the glass pushed in. This required complete removal of the meter to fix this problem. It's more difficult than it sounds because the ATD right-side panel can't easily be dismounted. Dealing with the nuts and washers that mount the meter requires some special tools. Once the meter was out, the housing and the glass were cleaned. The meter zero mechanism needed to be reassembled and then glued. The retaining ring for the glass had to be installed by pushing it evenly down to be against the backside of the glass. Then Cyno-A glue was sparingly applied to keep the ring in place. The meter was reinstalled. The one nut and washer on the lower inside has to have the washer super-glued to the nut and then, using a special tool that holds the nut/washer, it can be held in place and threaded by turning the screw in the front. The other two nuts are fairly easy to access and remount. 8-17-24 Thumb Screw for Ch.B Osc Adjustment Lock was missing. I found it inside the transmitter during disassembly. Luckily, it just screwed back in place and works correctly. Missing and Broken Fasteners - Several screws, lock washers and nuts missing. One broken screw on the Antenna-Sending relay board (K-103.) Enough of the threaded portion was left to allow gripping with flush type side cutters to get the piece unthreaded and removed so a new 4-40 BH screw could be installed. NOTE: I didn't notice until I doing the final assembly and mounting the rear panel that the lower-left corner 6-32 BH screw had been broken off and the remains were deep in the threaded hole. I may fix this later. I don't want to do any drilling, screw extraction and re-tapping with all of the tubes installed. |
Disassembled down to Main Frame - Cleaned spider webs and dead insects out of the left side area.
Right side was not as bad. Lots of spider webs though. Some minor corrosion. Cleaned
panels with Glass Plus. Minor straightening, especially on corners. Checked the 2 watt resistors
that are underneath (after dismounting the bottom cover) and all checked within
20% (even though marked 10%.) Every cavity of the main frame has insect debris
but it brushes out easily with a 1" wide soft paint brush or 1/2" paint brush
for smaller areas. Cleaned every part of the main frame, first with WD-40 and
then with Glass Plus. 8-17-24
Unobtainium Power Connector, a Solution that Works - The box connector is a Cannon NK-M8-32S - I assume the mating connector plug is Cannon NK-M8-32P but I can't find any source that has "32" size connectors. Original NOS or Used will have to be found. Until a proper connector can be located, the pins are .125" diameter and the same size as the tube pins on a five pin tube base. A fiber-type five pin tube socket has receptacles that almost surround the tube pins. These can be removed and used for the connection to the socket pins. Then proper size wires can be used for a cable. The pins will have to be insulated. When building the cable, it will have to be sleeved with copper braid for shielding. This cable will be six feet long so the PS (or dynamotor) can set on the floor if it needs to. UPDATE: Allpoints supplies a very nice push-on female wire connector that's for .125" diameter male pins. Wire solders to the rear of the pin and there's a wrap-around strap to support the wire/insulation. These are really perfect for this application. For some reason, these quality connectors are impossible to find locally but can be ordered online from Allpoints, pn 85-1075, at around $3.80 each. |
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Using the ART-13 AC PS to Operate the ATD - To operate the ATD using the "Homage a le Valve" ART-13 AC PS (without permanently modifying the PS's ability to also power an ART-13) will require using a special "ATD to ART-13 PS" cable that has to be built up. In the cable, ATD pin 1 (+28vdc) will be connected to ART/PS pin 3 (+HV/+LV relay) and ATD pin 4 to ART/PS pin 8 (chassis connection with PTT.) This allows the ATD's PTT or CW selection to turn ON the +HV and +LV transformer primaries providing these voltages in a manner similar to the dynamotor operation. In the cable, ATD pin 8 will be connected to ART/PS Pin 10 and will carry the +1000vdc. Additionally, -HV on ART/PS pin 2 should have a jumper to pins 5 or 9 to provide chassis-ground for the +1000vdc. ATD pin 2 will be connected to ART/PS pins 5 and 9 and will be the chassis-ground connection that will also ground the shield of the cable. ATD pin 5 will be connected to ART/PS pin 1 and will carry the +380vdc. ATD pin 3 will be connected to ART/PS pins 6 and 4 and will carry the +28vdc. All of these "cross connections" can be accomplished in the special-build power cable used between the ART/PS and the ATD. The cable will have soldered-on ring lugs on the ART/PS side and will have push-on pin female sockets for the ATD side. The wires for chassis-gnd and for +28vdc will be 14 gauge and the other four wires will be 16 gauge. Also, to eliminate the need to close ART/PS pins 7 and 5 to turn ON the +28vdc at pin 4 and pin 6, a jumper from pin 7 to pin 5 on the ART/PS rear terminal strip can be installed. This would result in the PS +28vdc relay being "on" during PS operation but that's the way it operates when powering an ART-13, so the jumper from pin 7 to pin 5 is an easy to install solution. The "jumper mod" is easily be removed when the ART/PS is used to power an ART-13. Of course, to power an ART-13, the ATD cable would be removed and the ART-13 cable installed. |
Logging Chart for Ch.B missing - The other three are
present so I can copy one of those onto a manila folder paper for the correct
color. I probably will have to glue to something for the replica to be the
proper thickness. These tags are mounted with two 4-40 screws and nuts -
requires that the module be "out of the transmitter." Tested the Two Audio Transformers - I used the schematic to determine where to access the primaries and secondaries for each transformer. Both the audio driver transformer and the modulation transformer tested okay. 8-18-24 Cleaned All of the Relay Contacts and the Contacts in the Main Frame for the Tuning Units - I used DeOxit applied with a saturated piece of paper that was drawn through the relay contacts to clean them. The stationary Tuning Unit contacts were cleaned with DeOxit applied with a small paint brush and then wiped with a paper towel (later these Tuning Unit points were cleaned more aggressively.) 8-18-24 Cleaned and Inspected Channels A through D Tuning Units - Mildly dirty, a few broken or missing screws. Slightly bent sheet metal on Ch. D air variable-C but it seems to have been that way since the original assembly. There's a flex-coupler on the shafts that compensates for the misalignment. Originally, the ATD came with a 540kc-1500kc module, a 1500kc-3000kc module and two 3000kc-9050kc modules installed. Mine has two 540kc-1500kc modules and is missing the 1500kc-3000kc module. One of the 540kc-1500kc Tuning Units has the only serial number that matches the main frame serial number. Channel C Tuning Unit - Broken screw head on rear bottom insulator panel (6-32 BH.) Removed the broken screw by removing the rear nut and washer so it could be pushed out of the hole. Installed new 6-32BH machine screw and installed the washer and nut. |
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Low Voltage Test - Applying +27vdc to the ATD - I used an old Meanwell +24vdc 13A
power supply with 14 gauge wires going to the Cannon NK-M8-32S connector. Pin 2
is chassis ground and pin 3 is +28vdc in. I used high-quality Allpoints 85-1075
push-on connectors that were soldered to the two wires and then pushed onto the
proper pins of the box connector. I installed all of the tubes, (1) 814, (4)
6L6G, (1) 12SL7GT and (1) VT-150. I switched OFF to PHONE-STANDBY position
and all of the tubes illuminated (except the VT-150, of course) and the BATT
position for the GRID Meter showed +27vdc when actuated. I confirmed that the
channel selection worked fine in manual. I then tried the motor drive channel
selector. It rotated very slowly and the forward-reverse contacts (S-101) started to
smoke. The load of trying to rotate the gear work was too much. I sprayed the
gears and bearings with WD-40 (a quick expedient for penetrating oil.) I also
cleaned the contacts on the forward-reverse switch. Now the motor drive ran
quite fast with just a very slight, normal load. But, although the motor would
stop on the correct selected channel, it wouldn't reverse direction if a "lower"
letter was selected, it would just continue to rotate forward and then stop on
the correct channel selected. There's a cam that should actuate the
forward-reverse switch that must be in the right position. Also, the
letter-wheel is slightly off, although it is within the window of the front
panel, it isn't in the center of the window but the cams for the channel select
are exactly in the correct position. This might just be a simple adjustment of
the letter-wheel position. I also checked the operation of the keying relay by
operating the KEY TEST switch and the K-103 relay operates correctly. 8-19-24 Motor Drive Channel Select - Read the Manual - I've re-read the manual several times and no where does it say that the motor runs in reverse if a "lower" letter is selected. I checked the sequence of the forward and reverse contacts and it looks like it does exactly what's described in the manual. The motor-drive is working great and stops perfectly on whatever selected channel is set. I'm wondering if the "reverse" operation on "lower" letters (an assumption on my part) isn't really what the "reverse" is for. I now think that the "reverse" motor winding actually seems to be for "stopping" the motor exactly in the correct position for the channel selected with no "over-shoot." 8-20-24 |
Restoring the Antenna-Gnd Mount - This piece bolts to the left side of the
transmitter and holds the insulator that has the Antenna input terminal and the
Receiver terminal. All three connectors are RAJAH types, like spark plug tips. The Ground terminal is connected to the mount and to the side
panel for the chassis connection. The paint on this metal mount is very, very
thick, like Japan enamel. On this ATD, the mount's paint was chipped and some
paint was missing. There also was some
corrosion on the metal mount. The engraved nomenclature looked like it was done
after the paint job since the engraving into the metal is fairly shallow. To
repaint, I had to remove the old paint. This proved somewhat difficult. Methylene-chloride
stripper would barely do anything. I chipped and scraped and then applied more
stripper and left that on the mount for one hour. This time I used a metal
bristle brush to remove the softened paint. This worked fairly well but I still
had to sand the remaining paint off of the mount. I went over the engraving with
a diamond tip graver to get it a bit deeper. It's just the way the original was
made however, that is, the engraving done after the paint job resulted in deep debossing that
was filled with white paint. However, the depth was almost all paint! Now that's
gone. If the new paint job fills the engraving, I'll just leave it that way. The
connections are pretty obvious anyway. 8-20-24 - I painted the mount with
several coats of Krylon Gloss Black. This really didn't fill up the engraved
nomenclature so I used various graving tools to "dig out" the paint. This left
the nomenclature silver and easily readable. In two places, the "D" in GND
and the "AN" in ANTENNA, were corroded to the point that the engraving
wasn't present at all, so these two areas were engraved by approximation
of what should have been there. Looks fine from a distance and
acceptable close-up. 8-21-24 Cleaned Antenna-side panels, remounted and resoldered Antenna buss wire. Until I get the RF Amp meter from Mike 'MS, I'm just going to connect the RF output directly to K-103, the sending/antenna relay. That way I can proceed with testing the ATD. The RAJAH bakelite spark plug terminal push-on connectors arrived today. These will be used to connect the antenna and ground to the ATD. 8-22-24 |
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Making the Power Cable - Chassis-Ground and +28vdc are 14 gauge
wires (+28vdc is Red and Gnd is Blue.) PTT is +28vdc Red 16 gauge and switched
to ground is Brown 16 gauge. +380vdc is 16 gauge Orange. +1000vdc is 16 gauge
Blue. The cable is approximately six feet long. The wires were slightly twisted
together and then wrapped with black electrician's tape. Then a braided copped
shield was harvested from RG-8U coaxial cable and sleeved over the ATD cable. A
small copper braid was soldered to each end for a ground connection on the PS
and on the ATD. Then the cable was again wrapped with black electrician's tape.
Ring lug terminals were soldered to the PS side of the cable. The ATD side has
Allpoint push-on connectors for +28vdc and Ground. I harvested the receptacle
pins from a fiber-type five-pin tube socket. These can be straightened and then
function quite well as push-on connectors. These were installed on the four 16
gauge wires. All of the push-on connectors were sleeved in fairly thick rubber tubing
for insulation. The color of the wires is used for ID purposes. The two blues
and the two reds are different shades and different gauge wire so there's no confusion. 8-23-24 ATD Dynamotor Arrives - I found an excellent condition (NOS, actually) ATD dynamotor for $70. It arrived today. I don't plan on running the ATD on the dynamotor just yet. If and when I move the ATD out to the shop, that's where I have the large PP-1104-C power supplies (three of them) for running high-current devices. I'll have to either modify the power cable I just made or build another. But first, the ATD needs to be running correctly on the ART/PS and operated "on the air" from upstairs. Before I actually used the dynamotor I would have to "service" it. After all, the grease in the bearings is over 80 years old. 8-23-24 Well, that plan changed,...read Dynamotor section further down. More ART/PS Changes - I checked the schematic and updates that I had made to this ART/PS a few years ago and found that I had changed the +400vdc to a pi-network filter to up the voltage and it was then running about +420vdc, too much for the ATD. I decided to put the +400vdc back to a similar configuration that I had before but without the input capacitor, in other words, a choke-input with dual filter chokes. This should produce about +380vdc. The choke input filtering gives better stability and at least a 10% reduction in output voltage. Test to confirm. I also brought in from the shop a roll-around small furniture dolly in order to have any easy way to move this ART/PS that weighs about 80 pounds. 8-24-24 |
+380vdc Test - I put 5000Ω load on the +LV output and the
resulting voltage was +380vdc. That's not a "full load" but I can't really find
what the current draw on the +380vdc is. The dynamotor data plate indicates the
+380vdc is rated at 400mA but I
don't know if that's how much current availability the dynamotor has or if
that's the +380vdc current load of the ATD. 8-25-24 +28vdc "ON" Relay - In looking at the ART/PS, the wire from the +28vdc "ON" relay (ART-13 pin 7) that connects to chassis-gnd to power the relay is the next terminal adjacent to the chassis-gnd terminal. Rather than have a second jumper, I just moved the ring lug over to the chassis-gnd terminal to provide the ground return for the +28vdc "ON" relay. Now there's only one jumper and that connects -HV to ground (ART-13 pin 2.) 8-25-24 Set-up and Operational Test - The manual has a step-by-step procedure for testing and set-up. This is probably the easiest way to find any additional faults. I had to move the ART/PS up onto a small table next to the test bench since I really couldn't see the output voltage meters or the indicator lamps with it on the floor. Out of the cabinet it probably only weighs about 65 pounds. 8-26-24 Throttle Switch and PTT Line Problems - The PTT line and the Throttle Switch wouldn't "lock" the sending relay K-103 in the transmit position. This problem was caused by K-101A on the Phone Relay having dirty contacts. I used DeOxit soaked paper pulled through the contacts to clean them. Then the PTT and Throttle Switch both worked correctly. 8-26-24 |
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Channel Select Contacts - The manual indicates that these can
be cleaned with "sandpaper" which sounds a little harsh. These contacts were
black with oxidation. Usually "black" indicates silver oxide which is very
conductive. I used a brass bristle brush to clean the black oxidation off anyway. The
brass brush only removes the oxidation and doesn't harm the plating on the
contacts. I cleaned both the modules and the main frame contacts. 8-26-24 More Testing Reveals Another Problem - The +380vdc under load measures +360vdc which is close enough. VT-150 glows purple when transmitter is operating. So far all testing is in the "TUNE" mode which prevents the +1000vdc from going to the 814 plate. I setup one of the 3000kc-9050kc modules for 4000kc operation. I connected a 50Z dummy load to the ANTENNA-GND terminals. There are four switches inside each of the four modules that have to be set correctly and then there are six front panel switches or controls have to be set correctly for the frequency of operation on each module. The ATD was set for CW operation. When the TEST KEY is switched, some PA grid current should show, however, the meter actually went negative. By tuning the MO PLATE, I could just get the meter to read "0." I happened to look at the 814 when I pressed the TEST KEY and the bottom half of the tube turned purple inside. This is a sure sign of a "gassy" tube, so no wonder the PA GRID current wasn't measuring as expected. I thought I had an 814 in my tube stock but I couldn't find it (if I ever had it.) I had ordered two of the cheapest 814s off of eBay. Neither of the tubes had been tested but the sellers thought the tubes were NOS. The first 814 had an open filament (got my money back on that one.) The second tube didn't show much emission in the TV-7 and did give a slight indication of being gassy but I thought it might work in the ATD (I didn't ask for a refund since a couple of weeks had passed before I actually tested the tube in the transmitter.) This second 814 was in the original box with the original wrapping and original paperwork,...naturally the seller thought the tube was NOS so it wasn't tested. But, it's gassy, and the purple glow was only with the +360vdc screen voltage applied (wonder what it would have done with the +1000vdc plate voltage applied?) The only way to proceed is to buy tubes that are tested and guaranteed. These two "cheapies" were a waste of time. I ordered another 814 that the seller provided the TV-7 test data information on. We'll see what happens with this tube when it arrives. Out of curiosity, I'm sure the "cheap-o" prices might be of interest, right? The open fil 814 was $15 and the second gassy 814 was $18. The tested 814 was $39. So, luckily, the 814 isn't an expensive tube but I wasted a lot of time and that's what was aggravating. 8-26-24 |
Making Replica Logging Charts - To make a replica logging chart I first copied
an original logging chart using a laser printer and copied it onto manila folder
heavy paper. I then used Titebond glue and added four more manila paper pieces
for the correct thickness. This sandwich of glue and paper was compressed until
the glue dried. I should have sprayed the laser copy with Matte Clear Krylon, but I didn't. Also, I should have punched the mounting holes in each
layer before gluing, but I didn't. Since Krylon wasn't used, the durability of
the laser printing isn't very good. Since I didn't pre-punch the holes I tried
drilling the holes but that forces cut paper into the sandwich of paper and that
spreads the edges. So, the replica wasn't perfect. It still looks just like the
originals, at least from a distance of a few feet. It's really very easy to make
another one after I buy some Clear Krylon and I'll have plenty of time since I
have to wait for the new 814 to be delivered. 8-27-24 The New 814 - The new 814 arrived on Friday 8-30-24. I tested it in the TV-7 and this one actually tested good. I couldn't get the old 814 out of the ATD unless I took the rear cover off. Luckily, I had only put about six screws in since I thought I might be taking it off again. With the new 814 I now had about 15mA of PA grid current that would easily peak with the MO Plate control as described in the test procedure. Next was to go to OPERATE. I had about 80mA of PA current showing but the Plate tuning brought that down to 40mA at resonance. I tried several adjustments but it acted like the antenna wasn't connected but the dummy load RF meter did show a few watts of output. I tried connecting two dummy loads in parallel to have about 25Z load, this didn't help, still about 30mA to 40mA at resonance. I checked the manual procedure and it indicated that without an antenna the PA current would resonate at 30mA, which it did. I then found in the front part of the manual that the expected antenna was a 25 ft "T" antenna and the antenna resistance at 3mc was expected to be just 1.3 ohms with a capacitance of 80pf. The 50Z dummy load (or 25Z in parallel) must look like there's no antenna connected. But, reading a little further, there's a section on loading "abnormal antennas" that indicates that the series capacitor can be switched out or the taps on the antenna L can be changed to allow matching unexpected antenna impedances. 8-30-24 The ATD has RF Output Now,...Sort of - Taking the manual's indication that abnormal antennas may require adjusting the tuning module differently, I tried a few other setting. The best results were with switch J set to 5 (this shorts out coil a portion of L603) and then place switch K to short out the Antenna Series Capacitor. I then set Control E to position 7 (L606 Antenna Load.) These setting allowed me to adjust the PA Plate current to just over 100mA. Control C PA Tune worked just like it should, that is, dipping the plate current at resonance. Now this was using the Harrison dummy load (47 ohms) which would be presenting a pure resistance antenna with no reactance. Apparently, the 25ft "T" antenna that was "normal" had a much higher C value that required more L in the tuner. Since I use an external matching device that presents a 50Z load with minimal reactance, I should get the same results running to the antenna. 8-31-24PHONE Operation and CW "On the Air" with Collinear Array on Harmonics - First I tried the Sidetone. I used 600Z phones but I didn't hear anything out of either jack. Next, I switched to PHONE and plugged in a Shure 102C carbon mike. I've used this mike many times and it has a good response. I could just barely tell that the PA was being modulated. I could see the plate current meter move a little. I had the signal (still on the dummy load) tuned in on the bench monitor receiver. I could hear some modulation but it was probably only 30%, barely detectable. The +380vdc is running at +340vdc under load. I didn't notice any change in the voltage as I spoke into the mike. The manual indicates that the +LV can be anywhere from +300vdc to +400vdc and since the dynamotor would vary in speed with the charging rate and engine speed, it would be expected that the dynamotor voltage would vary some. I tried connecting the ATD to the Collinear Array through the Viking Matchbox tuner. The tuner didn't show any change in the very high SWR. I added an auxiliary variable condenser on the Antenna output to ground (like the ART-13 uses) and I ended up switching the tuner to 40M. Now, I could get the SWR down to 1:1 and the PA current at 100mA. That gave me 35 watts to the antenna. I think if the screen voltage on the 814 was up to +380vdc or so, I'd be able to get more PA current and output. My concern though is that I've tuned the output network of the ATD to a harmonic of 3.974mc which would be 7.948mc and that's how I can get the tuner to achieve a 1:1 SWR on 40M but not on 80M. 8-31-24 |
Electrolytic Caps were
Defective - There are
two used in the ATD, C102 is the carbon mike bias voltage filter and C126 is the
Driver cathode bias filter to ground. Both caps are can-type electrolytics that
are 25mfd at 50vdc and are single capacitors per each can. Luckily, only one
wire connects to the positive terminal on each capacitor so isolating the old
electrolytic is easy. I used 33uf 50vdc radial type electrolytics. The + lead
was soldered to the isolated + wire and sleeved with black plastic tubing. The
negative lead was soldered to the ground terminal that the cap's negative
terminal was
connected to. This is the method used for both capacitors. The modern electrolytics are so small they can be tucked-away and hidden from view.
Tested the Sidetone on CW and the output to 600Z phones was clean and loud. I'll
have to reduce to Sidetone volume down to about 4, it was on 7 which is maximum
(and way too loud for phones.) I tested the ATD on PHONE and listened on the
Siemens model 311 monitor receiver. I was using the Shure 102-C carbon mike.
Modulation was strong and voice characteristics sound clear but like a carbon
mike normally sounds.
9-1-24 Experimenting with Various Antenna Coupling Capacitors - Since I was pretty sure that I had the ATD antenna coupling circuit tuned to 7.948mc instead of 3.974mc, I set all of the internal switches back to where they should be (G, H and J on 2 and K on 1.) Then, figuring that I had reduced the L in the module and got the loading to somewhat work (although on a harmonic,) the Collinear Array and Viking Matchbox must look like a lot of inductance until resonated and by adding capacitance in series, that might work. By switching K to 1, that added a series C already but it wasn't enough for a 50Z load. I tried 100pf first and this allowed the ATD to get kind of close to loading correctly but it required too much L that the module didn't have. I added another 100pf in series to have 50pf in series. This worked very well although I had to switch E to position 4 instead of 5. I could get a little over 100mA of PA plate current. I added another 50pf in series for 25pf. The results were about the same except switch E had to be in position 3. This switch E was adding L to the Antenna Loading which seemed to indicate I was close to finding a range of series C antenna coupling that worked. I think about 60pf or so would allow switch E to remain on 5 and I'd be able to get over 100mA of PA Plate current (later I was to discover that 100mA is way too much plate current.) I have to look through my high voltage capacitors to find a combination that will give me 60pf. OR, I have a box of NOS transmitting type air variables that are very small capacitance, probably 10pf unmeshed to 100pf meshed. Using one of those would allow "dialing in" what C works best. 9-1-24 |
Showing the electrolytic C102 Carbon Mike
bias filter |
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ART/PS Mods for the +LV
Supply - I noticed that as I
get the ATD closer to working correctly, the load on the +380vdc must be going
down some. The voltage is now running +350vdc under load. I can load the ATD to
about 110mA of Plate current and the "red line" is 120mA, so it's pretty close.
I'm pretty sure that if the 814 screen was +380vdc, I'd have the extra 10mA of
Plate current. I could easily remove the input choke from the circuit and then
move the electrolytic to be in parallel with the output electrolytic. This would
have a filter that is a choke input and a single large electrolytic on the
output. I've seen these used before but I'll have to test to see if the
filtering would be adequate (I doubt it.) The other test would be to just place
a shunt across the input choke and that would create a pi-network filter.
Voltage stability might be a problem but it would get the voltage up.
9-1-24 More Antenna Capacitor Testing - I tried the 100pf max air variable but the plates were too closely spaced and it arced at resonance. I have many other wide spaced air variables but the fixed high voltage caps are much easier to use. I tried 60pf and that was too much. I ultimately ended up with 37pf with the E switch on 3. I found that maximum output power doesn't happen with maximum PA plate current. At 110mA, I had about 25 watts output but at about 80mA I had 40 watts output. The SWR at the Matchbox is 1:1 so reflected power is zero. I suspect that when I raise the +340vdc (that is what it measures at 40 watts output) up to at least +380vdc, I should be able to have better efficiency in the 814 with higher screen voltage and I should be able to load up to 50 watts output on CW. 9-2-24 The ART/PS +LV Mod that Worked Best - First I tried connecting the +LV filter as a pi-network but the voltage was too high even under load (+420vdc.) Also, I had almost 20mA of PA grid current because of the high plate and screen voltages. Next, I connected the +LV filter as a single choke with output filter capacitor. Now, I was back to +340vdc under load. I listened to the signal on the monitor receiver and there really wasn't any change in the hum level. Then I thought about the capacitor. I had 20uf made up of two series 20uf caps at 10uf and a second series pair in parallel giving 20uf total. I had some 100uf 450vdc electrolytics that two in series would provide 50uf of capacitance. I added 750K balancing resistors to even out the voltage drop on the series electrolytics. With this hook-up, I had a consistent +360vdc under load in CW. 9-2-24 |
Using a D-104 Mike? - Why not? I set the mic switch to Magnetic (meaning dynamic) which is a 250Z input (same as the ART-13.) The D-104 is on an amplified base so the Z is much lower than a crystal mike and the gain can be adjusted as needed with the base's gain control. No problem in modulating the ATD. It sounded very good in the monitor receiver. While I had access to the Mic switch, I also set the Sidetone volume down to 4. ATD Reassembly - I installed the second 3000kc-9050kc module and set it up on CH. C to the same 3.974mc and made sure it loaded and performed the same as CH. D. I then installed the two 550kc to 1500kc modules but since these really aren't usable "on the air" I didn't do any setup on them. They are in channels A and B. I installed all of the panels and all of the screws with lock washers. More Antenna Capacitor Testing - I got to thinking that I had some doorknob capacitors that might work nicely for antenna caps. I found two 50pf, one 100pf and several others that were higher values that couldn't be used. By using the 100pf in series with one 50pf, I'd have 37pf and that should work very well. I used the RAJAH connectors and made one end of the capacitors able to plug into the ANTENNA terminal on the ATD using a short flex cable made out of copper braid and the other end of the caps were soldered to the coax center conductor of the ATD coaxial cable. The shield of the coaxial cable also had a RAJAH connector for the GND terminal. I then connected this cap-coaxial stub to a 50ft coaxial cable to run into the ham shack to connect to the Johnson Matchbox and the Collinear Array. This hookup allowed me to use the Drake W-4 wattmeter and the modulation monitor oscilloscope. With careful tuning, I found that the best setting was at 80mA of Plate current and that showed 48 watts on the wattmeter with a 1:1 SWR. |
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At this point the ATD is ready for its "On the Air" debut but I have to move it from the workbench to the ham shack. Not just that, but I have to make room for another station setup in the shack. I'm planning to initially use a Navy receiver with the ATD,...not the ARB,...I've tried that receiver on the air before and the lack of selectivity is a huge handicap for successful communications. I'm going to use the Hammarlund RBG-2 Navy receiver. This was a USN version of Hammarlund's HQ-120X that was specifically built for the Navy with heavy-duty construction, a slightly different tube line-up and different band spread calibration. I've used the RBG-2 on the air several times before and its a very capable receiver and very selective. One note though,...when I am given the Bendix RF Ampere meter, I'll be putting the ATD back on the bench for that installation. |
Operating the ATD "On the Air" |
Setup and Testing
- I first moved the ART/PS cabinet to the ham shack table. Then I
disconnected the ART/PS from the ATD and moved the PS chassis to the ham
shack. I then installed the chassis into the cabinet. I pulled the four
tuning units out of the ATD and moved the pieces separately. I connected
the ATD to the PS and installed all of the tuning units except Channel B
since that was where the motor drive was set. I moved the channel to D
and installed the B channel tuning unit. I made up some coaxial cable
using RG-8X. The 37pf series capacitor was inline as it had been for
testing. I also connected the antenna coax from the RGB-2 receiver to
the ATD. I was ready to apply power. The ATD powered up fine although there isn't any visual indication that the transmitter is "ON." The BATT V switch can be pressed and it should read +28vdc when the ATD is "ON." I was on CW so I switched on the high voltage at the PS. Pressing the KEY, I had about 85mA of PA Plate current. I checked the wattmeter and it read 55 watts. I think because the +HV is actually running about +1100vdc instead of +1000vdc (only 10% high) that's the reason that I have to load to a lower PA current. I reduced COUPLING slightly and dipped the Plate, I still had 55 watts. I reduced the ANT TUNING and dipped the Plate, now I had 50 watts at 75mA of Plate current. I went to PHONE and I connected the amplified D-104. Pressing the PTT, I still had 50 watts output. I reduced the COUPLING slightly and the ANT TUNING slightly and the power output dropped to 40 watts. I looked at the monitor scope as I talked into the mike. Lots of modulation but I don't seem to be going all the way down to cut-off. Negative modulation looks like about 80% maybe. Watching the +360vdc, it drops significantly with the voice peaks,...maybe down to +320vdc. Obviously, the current required for the modulator to really achieve cut-off is more than the ART/PS +LV can supply. I may bring in the HP713B power supply that can provide a solid +380vdc at 500mA and test the ATD in PHONE then. I would then have to do a few mods to the +400vdc supply in the ART/PS to get the current available up to 400mA or more. More Current Availability for the +380vdc Needed - Even though modulation isn't as potent as it could be, I think with the D-104 mike, the ATD will sound fine. After all, it's just the first "on the air" test coming up. The ART/PS upgrade can be another project in a week or two. I have a hefty 400vac CT transformer that must be good for at least 500mA. It measures as a 5.5" cube and has no other windings other than the 400vac CT and the primary. I'd have to look for a 500mA choke but I should be able to find one. I do have room on the ART/PS chassis if I rearrange some of the components. Not too much work - well, certainly not as much as building a complete PS. But, before I do that, I have to bring in the HP713B and verify that 500mA of available current will cure the wobbling +360vdc supply and allow 100% modulation. |
Dynamotor Operation
- Of course, an easy solution to the power supply current problem
is to use the original dynamotor. I have a very small +28vdc 27amp
switching PS that could easily(?) spin the dynamotor and not be loaded down
with varying current demands (this power supply alone couldn't supply
enough current to even start the dynamotor. At least 45 amps are
necessary to just get the dynamotor to spin with no load. I tested using
parallel-connected switching power supplies and while 40 amps wouldn't
spin the dynamotor, 50 amps did spin the dynamotor. At least 55 amps
would provide enough reserve for a fast start-up of the dynamotor
actuated by the ATD PTT but more current availability would certainly
help. More information in the "The ATD Dynamotor"
section further down this page.) The entire PS needs to be shielded
and the +28vdc cable from the PS to the dynamotor must also be shielded.
I'll only go this route if I can't find an AC PS solution that works.
One advantage to dynamotor operation is size and weight when compared to
the ART/PS. Arcing in the Unused Modules - I read in the manual about the unused modules causing problems if they are tuned to harmonics of the frequency being used. The cure is to retune them to a different frequency. I never tuned either of the 540kc-1500kc modules. So, I'll start by tuning one to 600kc and the other to 1100kc. Neither are harmonics to each other and neither are harmonics to 3974kc. I think I'll retune CH C to a different frequency than CH D. Maybe I'll set it up for 40M or easier would be 3995kc, an informal mil-rad net. When looking a little closer at one of the AM-BC tuning modules I noticed that four screws were missing. Two were completely gone and the other two had the screw head "popped off." These appear to be 5-32 screws but a 6-32FH fits fine and these screws, washers and nuts are only for the Garolite mounts for two of the coils. I installed the four 6-32FH screws using lock washers and nuts. 9-4-24 I thoroughly cleaned the contacts and the levers plus shot some DeOxit into the heads of the levers. I used a brass bristle brush and some DeOxit on a paper towel. I also cleaned the switch contacts G,H, J and K. Before installing the modules, I set one for 600kc and the other one for 1100kc. I set CH D for 3995kc and CH C is set to 3974kc. I tested the ATD and now there's no arcing. I had KØDWC (located about 2 miles away) listen to the transmitted PHONE signal from the ATD. I could also hear the signal over the telephone although there's a propagation delay of about half of a second that sounds like an echo. Other than a little feedback over the phone and the delay, the audio sounded good and Chuck also thought the ATD sounded good. I'll be giving the "ATD debut" on Sunday's (9-8-24) Nevada Mil-Rad Net on 3974kc at 0700hrs 9-5-24 |
ATD Debut Ends with a Problem - Propagation conditions were very good but attendance to the Nevada Mil-Rad Net was sparse. Still I got good reports from everyone. Although the +380vdc was running at +320vdc, the modulation levels seemed okay and the reports were that audio quality was good and modulation levels more than adequate. I made several transmissions but none were of any great length. Maximum length was probably about 3 minutes. During the "73 round" I noticed the PA Plate current dropped to about 50mA. A quick look at the PA grid current and it had dropped from 13mA down to 5mA. I still had a carrier according to the oscilloscope. I signed quickly as a "curl of smoke" appeared out of the right side vents. This seemed to indicate a burning resistor associated with a leaky or shorted capacitor. I disconnected the ATD and moved it to the workbench. I had pulled all of the tuning units. I checked the schematic to locate where the most likely resistors involved would be. I pulled the bottom cover and saw quickly that R121 had swollen and had cracks on top of the resistor body. This is the 1000 ohm plate load for the master oscillator although actually the voltage (+380vdc) is routed through R121 for all four channels and then the individual tuning unit selected will involve one of four 300 ohm resistors and then there's a bypass capacitor to ground on each of the 300 ohm resistors. These four bypass capacitors and R121 are always connected to +380vdc whether the channel is selected or not. I measured each bypass capacitor and C117 had a short to ground. The other three bypass caps involved all tested okay. I do remember that the arcing I heard did sound like CH A was involved and maybe it was. I wonder how long C117 had been intermittently shorting before it became a "hard short." |
Troubleshooting, Rework and Repair -
First, R121 is a huge CC resistor. It's the old style IRC 2W CC
resistors that are really quite large. I have a few of this size CC but,
of course, not a 1K value. I used two 2K 2W CC made by IRC (later
manufacture so these 2W are the same size as the old 1W resistors were) in parallel to have 1K at about 4W. It will do
until I can find one of these large IRC 2W carbon resistors in a 1K value.
Installation,...easy.
Second, accessing and removing C117 is made impossibly difficult due to the shield around the MO tube. With the 814 removed, one end of C117 is accessible but the other end is behind the MO shield. Although the shield might be removable, the mounting screws have washers and nuts that are covered by several MO components under the tube shelf. The value of C117 is .01uf and it's the standard "postage stamp style" cap with the yellowish-brown square body and the color-coded dots. I had several of these in the parts box. The color-code is probably the old RETMA code and has brown-black-black with a multiplier of red which equals 10,000pf or .01uf. Then there are two green dots for 5% and 500vdc rating. I found several .01uf square-package capacitors. I tested their working voltage up to +340vdc (max that the bench supply can achieve) and all caps handled the voltage fine. I chose the one that looked closest to the original. I lifted one end of the CH A MO plate load 300 ohm 1W CC resistor R148 and found that it too was cracked from overheating due to the shorted C117. I found some old style IRC 1W CC that were 390 ohm which is probably close enough. I couldn't get the soldering iron in behind the MO tube shield. I was going to take out the shield by removing the six screws, washers and nuts but I couldn't budge the screws (and I didn't want to break the screw heads off.) The nuts weren't accessible at all. I went back to trying to remove C117 by breaking one of the leads using a "soldering aid" tool but during the process, the solder lug broke instead. I had to use a different ground by adding a solder lug to a ground screw that was nearby. The parts were installed and they look like an original placement using original parts. I installed one of the 3000kc to 9050kc tuning units in CH D slot and applied power. I had 13mA of PA grid current, 90mA of PA Plate current and 50 watts output power. The +380vdc was +350vdc under load. Next, I installed the other 3000kc to 9050kc tuning unit and again I had 50 watts output with about 13mA of PA grid current. I installed both 540kc to 1500kc tuning units and then I had what appeared to be a short with no PA grid current. I pulled the BC tuning units and then the ATD went back to having full output. I plugged in one BC tuning unit at a time to determine which one was causing the problem. It was the BC tuning unit I had tuned to 1100kc. The problem is in the MO circuit of the tuning unit and that involves one tapped coil, a five-position switch, three capacitors and some wires. By selecting various switch positions 1 through 5, each of the three capacitors can be eliminated as the problem. That would leave the tapped coil or the wires. Since the rear lever switch shorts out the coil when the tuning unit isn't selected, it would seem that the coil could be eliminated. Since the AM-BC tuning units are virtually worthless and could never be used because their frequency of operation is entirely within the AM-BC band, perhaps the easiest approach is to remove P601 (a banana plug) which is the source of the +380vdc for the tuning unit. This, essentially, would eliminate the problem. The defective BC tuning unit will be replaced as soon as I find a 1500kc to 3000kc tuning unit, which would be usable on the 160M band. NOTE: When installing the "disconnected" BC tuning unit into the main frame, I noticed a very slight change in the "tune and load." It shows as a 5mA reduction in PA plate current. The load on the +380vdc doesn't change. A slight "touch-up" on the tuning of the two 3000kc to 9050kc modules was required. I think the proximity of any of the tuning units to the RF output buss wiring probably slightly changes the stray capacitance to ground and very slightly changes the "tune and load" settings. Once all tuning units are installed, the final "touch-up" seems to be consistent and remains at those settings. |
RF Amp Meter Conversion
- 9-14-24 - I picked up the RF Amp meter that came out of a Bendix
TA-12 from W7MS today at the Cabela's SNARS Ham Swap Meet in Verdi,
Nevada. Mike also included a bag with some extra bezels and an extra
spacer. This RF Amp meter, being for a TA-12, had a white scale while
the ATD RF Amp meter had a black scale. I had a "dummy" ART-13 RF Amp
meter installed in the ATD just to fill the hole.
Luckily, the TA-12 meter is a Weston 507 and the ART-13 meter is a Weston 507, so the scales are interchangeable. The scale swap was easily accomplished although the TA-12 meter needle needed to be white instead of black. I used a Sharpie White Paint Pen which is a very thin paint that covered the needle perfectly in one easily applied thin coat. The needle stops were missing on the TA-12 meter but present on the ART-13 meter. Essentially, between the two meters I made one black scale, 5 Amp RF current meter for the ATD. The top cover on the ATD had to be dismounted to have access to the RF Amp meter. Next was some work on the spacer which, of course, was for a TA-12. It wouldn't fit into the ATD without some involved modifications. The right side of the spacer had to be cut in order to have clearance for the metal frame's right side shielding of the ATD. This was accomplished carefully with a hacksaw followed by some dressing down with a file. This cut also was necessary for the meter flange. Then the left side had to have .250" of relief depth (removing spacer material) from about 200º up to about 350º for clearance of the ATD metal framework. Finally, about .190" of relief was necessary at the top (almost down to the threaded hole) and additional .250" relief depth from 5º to 20º to clear the upper framework. Once these cuts were made, the spacer fit correctly up flush with the back of the panel. The rebuilt meter was mounted to the spacer and then the entire assembly was mounted to the front panel using the original meter "flange bezel" the rear portion of which fits through the inside of the spacer and hides the spacer when viewed from the front through the bezel glass. RF Amp meter hook-up required a small section of 12 gauge buss wire because the original meter had been "cut out" leaving the existing buss wire too short to reach the meter. I used a crimp splice (with the plastic removed) and soldered it to make a junction between the original buss wire and the new section going to the meter. The original output buss wire I had connected to the sending relay that then switched to the ANTENNA terminal when transmitting. Now this buss wire had be connected to the meter. Then a new 12 gauge wire had to be run from the other meter terminal to the sending relay. That completed the hook-up. Operation - With a 50Z antenna load at a 1:1 SWR and only about 45 watts input, the Antenna Current shows about .4 amps, so the meter needle doesn't move very much. With a very low impedance antenna, such as an electrically short vertical, the current would read much higher. Also, the TA-12 white scale had a different projection than the black ART-13 scale so the actual accuracy of this RF Amp meter is compromised (most Antenna Current meters were just used a "peak output" indicators and not for calculating power output since the antenna impedance was probably unknown.) I noticed that with the RF Amp meter installed inline with the RF output now that some slight readjustment of the tuning modules was necessary. Not totally unexpected and the power output is still at 45 watts to 50 watts (measured with an external but inline wattmeter.) |
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Second Net Operation - 9-22-24 - I did a pre-net check out of the ATD loaded to 45 watts output into the Collinear Array at a 1:1 match. I was watching the oscilloscope that monitored the wave envelope sampled at the Johnson Matchbox. This time the waveform looked symmetrical with equal positive and negative modulation. The percentage of modulation still didn't appear to achieve cut-off or 100% negative but that's probably due to the +380vdc running at +350vdc and dropping to +330vdc during voice peaks. This is actually much better than the first "on the air" attempt. I monitored the signal quality by listening to the HRO-7T without an antenna connected and the RF gain reduced as needed. The audio quality sounded very good. So, I was ready for the net. W7MS was also going to run his ATD transmitter. Mike was running his ATD on the dynamotor and was routing the RF out to a Collins 30S-1 linear that boosted his RF level to 300 watts of carrier,...quite a signal. I was relying on the gain of the Collinear Array to help my 45 watts of carrier. I was using the USN/Hammarlund RBG-2 as the receiver. All stations were Q5. Although my signal reports for the ATD weren't as strong as normal, I did get between S7 and S9 from most stations, which is okay for 45 watts. The ATD was much more reliable this time. No problems. The RF Amp meter barely moves during transmission but that's expected with the 50Z low-reactance load of the Collinear Array. Later, I listened to Wavelength Radio's online recording of the net specifically to see the panadaptor display of the ATD signal. It still appeared to favor the upper sideband in the display but, interestingly, Mike's ATD also showed similar characteristics on the panadaptor. More investigation required after I have the ability to power up the ATD with the dynamotor so I have sufficient current available for the +380vdc. |
ART/PS +400vdc Redesign
- Re-thinking this Project
- In order to increase the current availability for the +380vdc, I'll
need to rebuild that section of the PS. I've found a 435-0-435vac
transformer that's supposed to be rated at 4 amps but that hardly seems likely since that's
about 1700
watts on each side of center tap. The rating is probably .4 amps or
400mA which is spec for the dynamotor current on the +380vdc. I've found two GE chokes that are rated at 435mA. I'll
probably only need one but, if I have room, I could make a dual choke-input
filter for better filtering. I've also found a 5vac filament transformer
rated at 10 amps although I really only need 6 amps. I'm going
to have to use two 5U4GB tubes in parallel to get the current available
up to 400mA. I'll need to punch another hole for another octal tube
socket. I have to remove the existing 400vac transformer, the two
chokes in that supply and the 5vac filament 3 amp filament transformer.
I'll have to move the +28vdc "ON" relay to a location under the
chassis. I'm going to move the +28vdc Lambda PS to the rear of the
chassis and orient it lengthwise. That will give me sufficient space for
the new components. I have to mount the 435vac CT transformer on its
side using a "L" bracket-type mount that has the long-side of the "L"
mounted to the chassis and then the transformer mounted to the
short-side of the "L." The transformer is 6.25" tall and
that's about .25" taller than the space I have above the chassis with the cabinet
lid closed. With a side mount using a "L" bracket, the transformer measures
5.625" tall.
THIS SOUNDS LIKE A LOT OF WORK! - I'm having second thoughts about this involved of a modification to the Homage a le Valve ART-13 power supply. So, for now,...further modifying the Homage a le Valve ART-13 PS has been halted. Now I'm going to take a look at the possibility of dynamotor operation,... |
Servicing the ATD Dynamotor
With all of the modifications required for the "Homage a le Valve" ART/PS, sometimes it seems that it would be easier to just use the dynamotor. The 27 amp +27vdc Lambda power supply doesn't provide enough current to even start the dynamotor. Though the manual indicates that about 20 amps is required for ATD-phone operation, this is "running current" - not "instantaneous starting current" - which obviously exceeds the capabilities of the 27 amp Lambda. However, there's an old trick of connecting similar power supplies in parallel to increase their current capabilities. I connected TWO 13 amp Meanwell +27vdc switchers in parallel with the 27 amp Lambda. I set all three PS outputs for +27vdc +/- 0.2vdc. In theory, I should have 53 Amps available. Will this actually work? Read on,... |
Servicing the Dynamotor
- Although this dynamotor appears to be NOS (and probably hasn't ever
been used,) that doesn't mean it would just power right up with +28vdc
applied. The bearings still have 80 year old grease inside and the
brushes have probably been setting in the same position on the commutators and in their brush-barrels since the early-1940s. All
"as found" dynamotors really need to be taken apart and examined first. If
everything looks good, then the commutators can be cleaned, the brush
surfaces cleaned, the bearings cleaned and relubed and any other clean-up
required performed. The component box should be checked. Only after this
servicing is performed can the dynamotor be powered up.
The end-bells on this dynamotor still have the mounting screws "safety-wired" and it's unfortunate that the wire has to be removed in order to dismount the end-bells to have access to the bearings, brushes and commutators. With the end-bells off, I could use the fan to manually rotate the armature to see if it would move and how much "drag" there was. The armature did move and the drag was considerable. Component box inspection turned up a leaky oil-filled capacitor. This was physically "leaking oil" not current leakage. Although it looked like a lot of oil it really wasn't. The residue was cleaned up with a Q-tip. This "weeping" of oil is common and usually isn't a problem if it's just the "weeping" type of leakage. The capacitor will have to be monitored from time to time to see how much (if any) oil leaks out. Everything else in the component box looked in good condition. All spare fuses and tools were present. Pulled all of the brushes. These were placed on a white sheet of paper in the proper orientation and placement for reassembly. Pulled the fan off of the shaft to allow access to the bearings and motor-side commutator. Pulled the bearing covers on both ends. Dried grease was obvious. I used WD-40 as a solvent to loosen and remove the old grease. I worked the WD-40 into the bearings on both sides by rotating the armature. At first, with the dried grease, the shaft was moderately difficult to turn and wouldn't "spin." After the WD-40 soaking, the armature spins easily. I let the WD-40 soak in the bearings all night. |
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The next day, I cleaned the commutators with 600 grit Al-Ox paper and
then washed the commutators with denatured alcohol. I repacked the
bearing using red wheel bearing grease and then reinstalled the bearing
caps. I checked the brushes and they looked new but a gave them a gentle
cleaning with a brass brush just to get any old dirt off. The brushes
were installed exactly in the positions that I had removed them from. I
cleaned the area around the commutators with denatured alcohol to remove
any old excess grease that had been "pushed out" by the repacking
process. This completed the servicing. A Tiny Power Supply for Dynamotor Operation - To power up the dynamotor requires at least 45 amps of starting current. I tried 40 amps and the dynamotor pulses, the relay chatters and the armature slowly rolls but never increases speed. At 53 amps the dynamotor starts right up and gets to full speed in about a half-second. Actually, these switchers will supply even more current "peak" for about ten seconds which is more than enough time to start up the dynamotor. The "peak" current available is about 65 amps. I used an old ART-13 dynamotor battery cable that I modified by reworking the connector. The ART-13 dynamotor uses pin 2 for +28vdc input while the ATD dynamotor uses pin 3 for the +28vdc input. I had to simulate the ATD PTT that "turns on" the dynamotor. For this I used two test leads,...one for +27vdc going to pin 1 and then ground going to pin 4. This connection actuates the dynamotor relay and starts the unit. I measured the voltage output with no load and had about +1050vdc on pin 8 and about +405vdc on pin 5. The test setup is shown to the right. I found the two spare Meanwell 24vdc 13A power supplies out in the shop. They're connected in parallel using 16 gauge wire to provide 26 amps. The Lambda PS is to the far right and it's connected in parallel to the Meanwell combo. The Lambda provides 27 amps. All three supplies were set to +27.02vdc (this was the highest voltage that one of the Meanwell would adjust to, so it determined the voltage setting for the other two supplies.) The output of the Lambda has the battery-type cable that has the ATD-Dynamotor connector on the other end (this cable is also shielded so it doesn't radiate any RFI.) Since the output of the +HV is +1000vdc, I couldn't use the Fluke DDM, I had to use the Triplett VOM to measure that voltage. I used a rubber mallet and a wooden block to remove a dent in one of the end bells. Then the end bells were touched-up with black acrylic paint and then installed. This completed the dynamotor clean-up and servicing. Note,...this is one LOUD dynamotor (like a big shop-vac) I was worried about the "screaming fan" on the Lambda PS,...I can't even hear it when the dynamotor is running. |
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What! Another Project? -
Since it seemed that 53 amps was probably about just 5 or 6 amps over
what was necessary just to get the dynamotor to spin with no load, I
wondered how the extra load of supplying the +28vdc necessary to power up the ATD
would affect the dynamotor operation. About 5 amps are required for the
+28vdc on the ATD alone. Each time the PTT is depressed, the dynamotor
would have to "start up" and that brings in the "instantaneous starting"
current issue. It would be nice to have a lot more "head
room" as far as current availability to smooth out the +28vdc
during the PTT actuation. Would it be possible to order two
more 24vdc 27amp Lambda power supplies? Yes, there are many listed on
eBay. Would it be possible to connect three of these type Lambda Power
Supplies in parallel and have the current availability be 81 Amps
continuous and 93 Amps peak? It
seems so. I've ordered the two additional Lambda power supplies and when
they arrive,...more experiments will reveal if operation of the complete ATD-dynamotor
system is possible with these tiny (but noisy) power supplies. In actual
operation, the high current would only be necessary to start the
dynamotor. As soon as the armature begins to rotate, the current demand
rapidly drops off. When running at speed, the maximum current draw is spec'd at
19 amps and that's the total current including the 5 amps of current
that is necessary for the tubes and relays in the ATD. However, the
instantaneous current draw for starting the dynamotor from a "dead stop"
can be quite high and has obviously been demonstrated to be between 45
and 50 amps,...and that's with "no load." So high current availability
is necessary for quick-starting with the PTT actuation and minimal
fluctuation of the +28vdc to the ATD. Construction
of an 80 Amp +28vdc Power Supply That's Physically the Same Size as the Dynamotor
- When the new Lambda power supplies arrived, I discovered that although
they had the same specifications, they were longer in length and not as
wide as the old 27A Lambda. One letter in the Part Number made the difference.
It doesn't matter as long as they all can provide 27A. I tested these new
supplies and they work fine. I had planned on using a
small BUD Industries cabinet that was NOS condition. It measured 12"W x
8"H x 9"D and it had an unused aluminum chassis that fit inside. However, with the different
dimensions of the two new supplies, this BUD cabinet is too small. But,
I have another unused cabinet that measures 8"H x 14"W x 9"D and it also
includes a chassis. But, thinking about the power supplies and their
fans and the cooling,...why use a cabinet? The power supplies can just
mount on top of the chassis. I had thought that due to the noise of the
dynamotor and the power supplies, I'd place both units under the desk.
There's plenty of space and lots of air available. The location would have the
direct noise blocked, the cables are long enough, etc., so just a chassis
for the PS
should be easy and will work fine. I plan on using 14 gauge wire for the AC input
connections and 10 gauge for the +27vdc 80A output. As mentioned above,
this high-current is only "momentary" but I want to make sure that the
IR drop is as low as possible and that's achieved with large gauge
wiring. The normal "running" current demand will be about 20A, so I'll
have plenty of "head room" and that should allow AM modulation voice
peaks to not affect the +380vdc very much.
Since the Lambda power supply chassis are all mounted directly to the aluminum chassis and the Ground terminal on each Lambda power supply is connected to the power supply chassis, the individual Ground terminals on each power supply don't have to be routed to the AC ground wire terminal. But, the AC power cord Ground wire is connected directly to chassis in two places one of which is a lug under one of the Lambda power supplies mounting screws. The AC input to each power supply uses a soldered ring lug to connect the 14 gauge wires to Line and Neutral. There isn't a power switch or fuse in the AC input line. The AC line "bounce" is very noticeable when powering up the dynamotor so a switch and fuse would just limit the available AC line current somewhat. The 80A PS would only be plugged in when it's being used. The DC output of each Lambda was then adjusted to +28.0vdc BEFORE the three
were connected in parallel. I tried to get
the output voltages exactly the same from each supply for equal
distribution of the current carrying ability (within +/- .002vdc.) The DC output terminal block was made from two
pieces of .25" thick delrin with 1/4x20 brass studs and brass nuts and
washers to act as the high current output connections. The clearance holes through
the chassis for the DC terminal block studs were .750" in diameter. The 10 gauge
wires were soldered directly to the back end of the DC output studs. The
power supply end of the 10 gauge wires had ring lugs soldered on and
then these were attached to the PS output terminal strip. The wires were
routed through the chassis by way of grommet-lined holes.
Running the ATD on the Dynamotor - The end of the ATD power cable (that had connected to the ART-13 AC PS) had to be modified to use plug-in wire sockets since I don't have an original connector. I removed the ATD cable from the ART-PS. I then clipped off the ring lugs and cut the six wires all to the same length. I salvaged the receptacles from an old six pin fiber board tube socket to make suitable push-on female pins for the cable. The connections are easy for the dynamotor to ATD cable since both box connectors are identical and have the same connections, that is, pin 1 to pin 1, pin 2 to pin 2, etc., the colors of the wires can be used for reference. Also, in this cable two wires are 14 gauge for the +28vdc in and the Chassis-Gnd. The other wires are 16 gauge for PTT, Dynamotor Relay return, +380vdc and +1000vdc. The wire push-on sockets were covered with rubber tubing for insulation. The shield of the cable is connected to the chassis of the ATD on one end and to the Dynamotor housing on the other end. Since the ATD Dynamotor sounds like a very large shop-vac when running and the 80 amp power supply has three fans running, both of these units were placed under the operating desk. The cable is long enough and there's plenty of room under the desk. I did this the last time I ran a large dynamotor in the upstairs shack (the RU-16/GF-11 set up) and it really does quiet-down the operation.
As mentioned, I had to modify the ART-13 dynamotor cable to
work exclusively with the ATD dynamotor. I have another
ART-13 dynamotor cable, so changing this one to an exclusive ATD dynamotor cable
wasn't a problem. Incidentally, the two large wires in the ATD Dynamotor
Cable are 8 gauge wires. I connected up everything under the desk and
applied 120vac to the 80A-PS and it came up fine. I used the Throttle
Switch to energize the ATD dynamotor. It takes about 1.5 seconds for the
armature to come up to full speed. The Grid Current and Plate Current meters
don't just "jump" to the proper current, they "ramp up" as the dynamotor
comes up to speed. I had about 48 watts output with a 1:1 SWR match and
the PA Plate Current was 75mA.
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Adding a Linear Amplifier |
Sometimes the ATD's 40 watts out doesn't seem to be enough power,
especially on 75M,...even using the Collinear Array antenna. I do have the "W6MIT 95" homebrew linear amplifier that
could be used to increase the RF power. I have a 3db attenuator good for
about 30 watts and also a 6db attenuator good for 150 watts. The linear
amplifier is limited to about 18 watts input for the 100% duty cycle of
an AM signal and that results in about 140 watts output (25% of maximum
output capability.) Loading
the ATD for its rated 40 watts for PHONE would result in 20 watts drive
if the 3db attenuator was used. If I loaded the ATD for 45 watts that
would result in 11.25 watts drive if the 6db attenuator was used. It
seems that the 3db attenuator would work best. Since only about 20 watts
has to be dissipated the 30 watt rating of the 3db attenuator should be
sufficient. Like most high power attenuators, the 3db attenuator uses
male and female N-type connectors. The input to the Linear Amp uses a
BNC connector. Connector-adaptors are necessary for the RF output cable from the ATD
to the attenuator and from the output of the attenuator to the Linear RF
input. The coax from the ATD is about 10 feet long so I'll need about
another 10 feet of RG-8X to run to the
attenuator/Linear combination. The Linear already has the proper coax to
route the output to the Johnson Match Box/Collinear Array. The other
problem is how to actuate the Linear when the ATD PTT is energized. I
thought about using the PTT line accessed at pin 11 of the REMOTE where
the PTT "floats" at +28vdc and is taken to ground when PTT is activated.
It would be possible to use a small relay with one end of the 24vdc coil
connected to the +28vdc power at REMOTE pin 13 and the other end of the relay coil
connected to the PTT line at REMOTE pin 11. This would "switch" the relay with the PTT
actuation. The relay contacts could be routed to the Linear Control.
It's almost as easy (and quicker) to just run the Linear Control line to
a switch located by the ATD and just activate the Linear that way.
More coming,... |
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